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[Case studies] for Car hood manufacturing defects

Analyzed by the 4M framework (Man, Machine, Material, Method) and resolved using quality tools


Car Hood Manufacturing Defects: 4M Analysis & Solutions

(Each case maps a defect type to a root cause (4M) and corrective action with results)

Case

Defect Observed

4M Root Cause

Quality Tool Used

Corrective Action

Result

1

Dents in hood panels

Man: Improper handling by operators.

5 Whys

- Added foam padding on workstations.


- Training on "2-hand carry" technique.

Dents reduced by 85%.

2

Weld splatter marks

Machine: Weld gun misalignment.

SPC (Control Charts)

- Calibrated weld guns every shift.


- Added real-time monitoring.

Splatter defects down 70%.

3

Paint adhesion failure

Material: Contaminated primer.

8D Problem-Solving

- Supplier audit + batch testing.


- Revised storage SOPs.

Warranty claims dropped 60%.

4

Hood warping post-oven

Method: Uneven heating in curing oven.

DMAIC (Six Sigma)

- Redesigned oven airflow (DOE optimized).


- Added IR sensors for temp uniformity.

Warping eliminated (CpK >1.67).

5

Gap misalignment

Machine+Method: Fixture wear + loose SOPs.

Kaizen + FMEA

- Replaced worn fixtures.


- Updated control plan with 3x/day checks.

Gap compliance reached 99.2%.

4M Breakdown with Automotive Examples

  1. Man (Operator)

    • Issue: Scratches from jewelry/tools.

    • Solution: Poka-yoke (tool-less gloves + magnetic wristbands).

  2. Machine

    • Issue: Stamping press overloading.

    • Solution: Predictive maintenance (vibration sensors + IoT alerts).

  3. Material

    • Issue: Thickness variation in aluminum sheets.

    • Solution: Supplier SPC + incoming inspection gates.

  4. Method

    • Issue: Inconsistent torque sequence on hinges.

    • Solution: Digital torque wrenches with step-by-step guides.


Quality Tools Linked to 4M

Tool

Best for 4M Category

Example Application

5 Whys

Man

Rapid RCA for human errors (e.g., misloading).

FMEA

Machine + Method

Risk-ranking oven failures or stamping cracks.

8D

Material

Contaminated paint from supplier resolution.

SPC

Machine

Monitoring press tonnage stability.

Kaizen

All 4Ms

Quick wins (e.g., ergonomic workstation redesign).

Outcomes

  • Cost savings: $250K/year from reduced rework (Case 4).

  • IATF 16949 compliance: All cases closed with documented CAPAs.

  • Customer PPM: Improved from 1,200 to 150 PPM (Cases 1+3).


Visual Workflow for Defect Resolution

text

Defect → 4M Analysis → Tool Selection → Countermeasure → Standardize  

Example: Hood dents → Man (handling)5 Whys → Foam padding → Updated work instructions.

Need detailed templates (e.g., 4M checklist, FMEA worksheet) or DMAIC project reports for these cases

 
 
 

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